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Home > A-Series EFI / Injection > EFI Testing - Dyno Day 6: 1.5:1 Ratio rockers | |||||||
608 Posts Member #: 1106 Post Whore Hungerford, Berks |
28th Jan, 2019 at 07:47:52pm
As previously mentioned, I have mostly been running on the road at around 142KPA (6PSI) since installing the new “X7” manifold.
’77 Clubman build thread
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608 Posts Member #: 1106 Post Whore Hungerford, Berks |
28th Jan, 2019 at 07:48:42pm
The next thing that I found to play with was the exhaust system.
’77 Clubman build thread
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6745 Posts Member #: 828 Post Whore uranus |
28th Jan, 2019 at 08:27:06pm
excellent work graham.... well done . Medusa + injection = too much torque for the dyno ..https://youtu.be/qg5o0_tJxYM |
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2909 Posts Member #: 83 Post Whore Glasgow, Scotland |
29th Jan, 2019 at 01:21:45pm
loving this. turbo 16v k-series 11.9@118.9 :)
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Site Admin 15300 Posts Member #: 337 Fearless Tom Fenton, Avon Park 2007 & 2008 class D winner & TM legend. |
29th Jan, 2019 at 02:13:52pm
Great stuff. On the torque steer have you gone to rose jointed arms? As any compliance in bushes can magnify the effects of torque steer.
On 29th Nov, 2016 madmk1 said:
On 28th Nov, 2016 Rob Gavin said:
I refuse to pay for anything else Like fuel 😂😂 |
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Forum Mod 10980 Posts Member #: 17 ***16*** SouthPark, Colorado |
29th Jan, 2019 at 04:42:49pm
Fantastic details. This is good stuff. On 17th Nov, 2014 Tom Fenton said:
Sorry to say My Herpes are no better Ready to feel Ancient ??? This is 26 years old as of 2022 https://youtu.be/YQQokcoOzeY |
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608 Posts Member #: 1106 Post Whore Hungerford, Berks |
30th Jan, 2019 at 08:53:54am
Thanks for the positive feedback gents.
On 29th Jan, 2019 Tom Fenton said:
Great stuff. On the torque steer have you gone to rose jointed arms? As any compliance in bushes can magnify the effects of torque steer. No Tom, I did not get the rose jointed lower arms. But that looks like it can be remedied easily. The lower arms are from Minispares and they supply the rose joint kits separately, so can be swapped out. The question is, do I go to rose joint tie bars while I am at it? Spring Project list: -Fit rose joints on front suspension -Replace air filter to hopefully help with MAF signal. Also the replacement filter has a bigger surface area, so I hope to get rid of the very minimal vacuum I am seeing at high rev’s/ MAP. -Making some fairly major modifications to the inlet plenum and runners. -Install 4 port Waste gate actuator control solenoid and re-install dual port Waste Gate actuator with 10PSI spring. Edit - removed question about Exhaust valve sizes until I have done a bit more research. Edited by Graham T on 30th Jan, 2019. ’77 Clubman build thread
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608 Posts Member #: 1106 Post Whore Hungerford, Berks |
23rd Feb, 2019 at 01:47:50pm
Well, as the weather turned out nice over the last couple of days I decided on impulse to get back on the Dyno to see what changes, if any, the new exhaust and change in wastegate actuator made before I start making yet more changes.
’77 Clubman build thread
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971 Posts Member #: 3228 Post Whore North of the Netherlands |
23rd Feb, 2019 at 01:57:37pm
Thats a truly great result; well worth the efforts! Dazed and Confused.... |
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608 Posts Member #: 1106 Post Whore Hungerford, Berks |
23rd Feb, 2019 at 07:47:48pm
Now, the above looked good, but right at the end of the session a kind of red mist descend on me and I felt the need to progress past ~160 BHP, so I suggested to Robert maybe we could turn up the boost Fractionally for the last 15 minutes
’77 Clubman build thread
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6745 Posts Member #: 828 Post Whore uranus |
23rd Feb, 2019 at 09:58:32pm
That 230 lbs/ft on 17 psi or whatever it was is just incredible .
Medusa + injection = too much torque for the dyno ..https://youtu.be/qg5o0_tJxYM |
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608 Posts Member #: 1106 Post Whore Hungerford, Berks |
24th Feb, 2019 at 08:33:36am
On 23rd Feb, 2019 robert said:
That 230 lbs/ft on 17 psi or whatever it was is just incredible . . Looks like we still have an offset on boost. According to my data it was at 15.7PSI, according to yours it was 17PSI. But ultimately it’s about 8Lbs/ft and 7BHP per 1PSI boost. to spot any detonation..
??? It went weeeeeeeeeeeeeeeeeeeeeeeeeeee POP… ....the rate of boost rise was phenomenal.
This was another topic yet to come. Very briefly for now, we are not able yet to get the same boost rise when running on the dyno to what I experience on the road, regardless of which inlet manifold or even boost level. Therefore a big part of Friday’s Session was actually trying to get data to try to understand that. Below shows the comparisons in boost rise with revs, on dyno sessions and on the Road (always 4th Gear pulls on the road, which is why they are so short) So, I am convinced there is more there low down, but it’s how to get there. On Friday we tried different simulated loads – I think, but Robert will correct me, we have used 1000Lbs normally, but on Friday we tried both 1400LBS and then 1800Lbs. I have not yet converted the data from these sessions, but there was a good difference in rise of boost between 1000Lbs and 1400Lbs runs, but very marginal between the 1400Lbs to 1800Lbs run. I will get that data sorted ASAP. ’77 Clubman build thread
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608 Posts Member #: 1106 Post Whore Hungerford, Berks |
25th Feb, 2019 at 09:45:21am
So, it appears that the Plenum did split…
’77 Clubman build thread
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6745 Posts Member #: 828 Post Whore uranus |
25th Feb, 2019 at 11:09:14am
thats a big crack ! Medusa + injection = too much torque for the dyno ..https://youtu.be/qg5o0_tJxYM |
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608 Posts Member #: 1106 Post Whore Hungerford, Berks |
25th Feb, 2019 at 08:24:15pm
Yes, it looks like a fairly large crack in the plenum, but I’ve not cleaned it down properly yet to see what has actually happened to it and to what extent.
’77 Clubman build thread
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6745 Posts Member #: 828 Post Whore uranus |
25th Feb, 2019 at 08:40:32pm
looks like the head lifted due to not enough clamping graham . Medusa + injection = too much torque for the dyno ..https://youtu.be/qg5o0_tJxYM |
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608 Posts Member #: 1106 Post Whore Hungerford, Berks |
26th Feb, 2019 at 07:47:10pm
Ok, thanks Robert.
Edited by Graham T on 26th Feb, 2019. ’77 Clubman build thread
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5988 Posts Member #: 2024 Formally Retired Rural Suffolk |
27th Feb, 2019 at 09:06:21am
Interesting that the main gasket failure mode (where the fire ring was deformed outwards) is where the bulk gasket material is weakened by a relatively large un-supported hole.
Schrödinger's cat - so which one am I ??? |
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608 Posts Member #: 1106 Post Whore Hungerford, Berks |
28th Feb, 2019 at 08:32:08am
Well, I have an 11 Stud ARP set on the way, so I guess I might as well convert it to 11 Stud while it is all in pieces.
’77 Clubman build thread
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6745 Posts Member #: 828 Post Whore uranus |
28th Feb, 2019 at 09:53:25am
good work big boy , maybe a steel tube welded to a plate you can bolt to the deck , and then drill down the tube to keep it square ? Medusa + injection = too much torque for the dyno ..https://youtu.be/qg5o0_tJxYM |
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608 Posts Member #: 1106 Post Whore Hungerford, Berks |
28th Feb, 2019 at 10:07:31am
I was reading through some of the Threads I found yesterday on the subject and I think it was Wil_H that posted that he drilled the head first, then used the head bolted back on the block as a guide to keep the drill in line.
’77 Clubman build thread
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5988 Posts Member #: 2024 Formally Retired Rural Suffolk |
28th Feb, 2019 at 11:17:30am
We did it decades ago to another engineer's Mini back when I was in charge of the mechanical workshops at Bradwell - so had the benefit of some industrial size pillar drills.
Schrödinger's cat - so which one am I ??? |
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8604 Posts Member #: 573 Formerly Axel Podland |
28th Feb, 2019 at 11:24:46am
Some excellent results. Thanks for sharing.
Saul Bellow - "A great deal of intelligence can be invested in ignorance when the need for illusion is deep."
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608 Posts Member #: 1106 Post Whore Hungerford, Berks |
28th Feb, 2019 at 01:41:17pm
On 28th Feb, 2019 Rod S said:
…Head first using a template taken from a genuine "S" head then machined a bit of brass rod into a sleeve with the OD of the hole in the head and the ID of the tapping drill so, with the head bolted on it self centred the tapping size drill… Yes, I had thought about this also, but I have nothing to make a sleeve and unlikely to get anything for the weekend. But I’ll take a look see what I can get. On 28th Feb, 2019 Rod S said:
Also, I might be getting confused, but I think I read somewhere one of the conversion kits uses a smaller diameter stud at the thermostat end (to reduce the risk of it breaking through) ??? I’ve not received the parts yet, but the description for the APR stud set says: “7 x Short Head Studs (Disregard 2 if you're using a 9 stud application) “ So I assume from that they are the same size. ’77 Clubman build thread
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12307 Posts Member #: 565 Carlos Fandango Burnham-on-Crouch, Essex |
28th Feb, 2019 at 01:43:20pm
on the ARP kits I have used yep they are all the same diameter, (5/16?) On 28th Aug, 2011 Kean said:
At the risk of being sigged... Joe, do you have a photo of your tool? http://www.turbominis.co.uk/forums/index.p...9064&lastpost=1 https://joe1977.imgbb.com/ |
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Home > A-Series EFI / Injection > EFI Testing - Dyno Day 6: 1.5:1 Ratio rockers | |||||||
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